Technical information
imposing an excessive force on the position sensor. The force is great enough to loosen
the lock nut on the position sensor and allow the sensor to rotate.
Fix
The peak-peak displacement of the axle bolt was measured, throughout the joints range of
motion, and compared to the flexible range of the coupling. It was decided that the
potentiometer may be able to physically withstand the increased frictional force if it was
restrained. Although the lifetime of the part may be reduced, restraining the
potentiometer is the most cost effective solution at this time. The potentiometers were
fixed to there mount using a Loctite brand hardening epoxy. The system was tested and
physical movement previously observed between the potentiometer and mount was not
detected.
May 2001
Report
The right joystick is not responding.
Problem
The machine runs fine from the left joystick. The right joystick is determined to be
defective.
Fix
The joystick was sent to the factory for repairs.
November 2001
Report
The joint between the short arm and the long arm broke.
Problem
The axle bolt was broke during operation. It is unclear how or why the joint was
damaged; however, it is assumed that the operator may have caused the precrush door to
close on the joint causing the damage.
Fix
The joint was disassembled and a new axle bolt was fabricated. The axle bolt is a grade 8
bolt that is modified to interface with the position sensors. The joint was reassembled
and the position sensor calibrated.
February 2002
Report
There is low clearance between the clamshell and the dump body. In addition, automated
motion is being halted and responding erratically.
Problem
Copyright 2011, AHMCT Research Center, UC Davis