Technical information

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Therefore, a battery charging isolation system was added including two additional heavy
density batteries. The additional batteries allowed more energy to be stored, while
driving to and from the work zone, and used during the short time use of the ACM
equipment. The system was tested repeatedly and found to be a sound solution.
The cone stowage assembly on the ACM was an area that required frequent inspection
and maintenance. Due to the increased interest in extended field testing, it was decided
to modify the design to increase the robustness of the assembly. There were two
components on the stowage assembly that required high maintenance, the v-track rollers
and the main radial-load flat track rollers. The flat track rollers were simply undersized
for the mechanical loading encountered and would be replaced with a larger one.
Therefore, a new gripper assembly had to be built to accommodate a larger roller. The v-
track rollers were splitting due to higher than expected torsional loading on the gripper
assembly. The addition of a third track providing support on the top of an existing flat
track roller greatly reduced the torsional loading on the v-track rollers. The two
improvements to the gripper assembly have improved the robustness of the stowage
assembly and greatly reduced the required maintenance.
Prior to continuing field testing, new cones were ordered, according to the latest Caltrans
specification, and installed on the machine. However prior to installation, the rubber feet
on the cones had to be removed, as required by the current ACM design. The new cones
were more pliable than the previous cone. The pliability affected several parts of the
cone placement and retrieval process; however, the detection and grabbing of the cone in
the secondary funnel area was problematic. The upper portion of the cone periodically
collapses, sliding under the secondary funnel, allowing the base of the cone to get trapped
behind the flag of a limit switch. This configuration prohibits the cone from being
detected or retrieved. Therefore, new flag geometry was developed that eliminated the
possibility of a cone being trapped and undetected. The new design was tested and
worked effectively.
Testing in Santa Cruz on highway 1 with Granite Rock Construction Company was an
excellent opportunity to observe the interaction of the ACM with congested traffic. The
distraction to drivers of having an interesting automated machine operating next to them
and the physical obstruction of the ACM drop box were two areas of concern to
investigate. It was found that neither of the concerns were problematic. Most drivers
never even noticed that the ACM was working autonomously. In addition, the protruding
drop box did not appear to be problematic.
Caltrans conducted further testing of the ACM in the Livermore and San Jose areas. On
the freeways the machine also performed great. The only real concern was the spacing
accuracy of the cones. This is a known problem and is limited by the physical speed at
which the ACM components can operate and the speed of the vehicle. With a little
practice the operators were able to speed up or slow down their driving to get a more
desired spacing.
Copyright 2011, AHMCT Research Center, UC Davis