User guide

13-2
FlexPak 3000 DC Drive Software Reference
F00002
TACHOMETER
LOSS
Tachometer or encoder feedback signal missing.
Possible causes:
Tachometer or encoder coupling failure.
Disconnected, loosely connected, or damaged tachometer or encoder
wires.
Pulse encoder supply voltage low.
Incorrect analog tachometer scaling.
Incorrect pulse encoder configuration.
Motor armature winding not connected or open circuit.
Blown inverting fault (DC) fuse.
Inverting fault breaker tripped.
High inertia loads and high inductance armature circuits. To reduce
nuisance faults, increase the firing angle threshold (see section 13.2).
Tachometer or encoder failure.
F00003
OVERSPEED
Motor speed exceeded the 110% of
TOP
SPEED
.
Possible causes:
Incorrect tachometer or encoder scaling.
Blown field supply fuse(s).
Improper speed loop tuning.
PULSE
TACH
QUADRATURE
set to
ON
for a non-regenerative drive.
Incorrect pulse encoder wiring.
F00004
FIELD
CURRENT
LOSS
Standard or enhanced field supplies: The field loss detection circuit does
not sense any field current flowing in the motor shunt field.
Field Current Regulator kit field supply:
FIELD
FEEDBACK
(P.589) fell below
the
FIELD
LOSS
THRESHOLD
(P.512).
Possible causes:
Motor field winding not connected or open circuit.
Blown field supply fuse(s).
Blown AC line fuse(s).
Field supply failure.
Disconnected, loosely connected, or damaged wiring harness.
Field Current Regulator kit only: Improper field loop tuning.
Table 13.1 – Fault Codes (Continued)
Code OIM Display Description