Datasheet

LT3434
22
3434fb
APPLICATIO S I FOR ATIO
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Figure 14. Overall Loop Response
Figure 13. Model for Loop Response
catch diode and connecting the V
C
compensation to a
ground track carrying significant switch current. In addi-
tion the theoretical analysis considers only first order non-
ideal component behavior. For these reasons, it is important
that a final stability check is made with production layout
and components.
The LT3434 uses current mode control. This alleviates
many of the phase shift problems associated with the
inductor. The basic regulator loop is shown in Figure 12.
The LT3434 can be considered as two g
m
blocks, the error
amplifier and the power stage.
Figure 13 shows the overall loop response with a 470pF V
C
capacitor and a typical 100µF tantalum output capacitor.
The response is set by the following terms:
Error amplifier: DC gain is set by g
m
and R
O
:
EA Gain = 650µ • 1.5M = 975
The pole set by C
F
and R
L
:
EA Pole = 1/(2π • 1.5M • 470pF) = 226Hz
Unity gain frequency is set by C
F
and g
m
:
EA Unity Gain Frequency = 650µF/(2π • 470pF)
= 220kHz
Powerstage: DC gain is set by g
m
and R
L
(assume 10):
PS DC Gain = 6 • 10 = 60
Pole set by C
OUT
and R
L
:
PS Pole = 1/(2π • 100µF • 10) = 159Hz
Unity gain set by C
OUT
and g
m
:
PS Unity Gain Freq = 6/(2π • 100µF) = 94kHz.
Tantalum output capacitor zero is set by C
OUT
and C
OUT
ESR
Output Capacitor Zero = 1/(2π • 100µF • 0.1) = 15.9kHz
The zero produced by the ESR of the tantalum output
capacitor is very useful in maintaining stability. If the ESR
of the output capacitor is low or better transient response
is required, a zero can be added to the loop using a resistor
(R
C
) in series with the compensation capacitor (C
C
). As
+
CURRENT MODE
POWER STAGE
g
m
= 6
g
m
= 650µ
1.25V
V
C
LT3434
ERROR
AMP
1.5M
R
C
R1
FB
12
11
SW
SW
2
5
ESR
OUTPUT
R2
C
OUT
3434 F13
C
FB
C
F
C
C
FREQUENCY (Hz)
0
PHASE (DEG)
120
80
40
160
180
–80
GAIN (dB)
0
40
–40
80
100
100 1k 10k 100k
3434 F14
1M10
V
OUT
= 3.3V
C
OUT
= 100µF, 0.1
C
F
= 470pF
R
C
= 10k
C
C
= 4700pF
I
LOAD
= 1A
the value of R
C
is increased, transient response will
generally improve but two effects limit its value. First, the
combination of output capacitor ESR and a large R
C
may
stop loop gain rolling off altogether. Second, if the loop
gain is not rolled off sufficiently at the switching frequency
output ripple will perturb the V
C
pin enough to cause
unstable duty cycle switching similar to subharmonic
oscillation. This may not be apparent at the output. Small-
signal analysis will not show this since a continuous time
system is assumed.
When checking loop stability the circuit should be oper-
ated over the application’s full voltage, current and tem-
perature range. Any transient loads should be applied and
the output voltage monitored for a well-damped behavior.